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250cc and Above Engine Tech Technical Discussion Forum for 250cc and up Engines |
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#1
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bogging down at less than half throttle
Been playing with the reaction 250 since I got the muffler welded on. It seems to run pretty good at wot, but when I let off the gas and give it less than half throttle it seems to bog down. Not sure if this is due to a rich pilot jet? I believe I put a 38 pilot in when I added the ported polished shaved head, uni, and exhaust. Any ideas? Also I was having issues trying to adjust my valve lashings but I thought I had gotten them set pretty good. I tried adjusting the pilot screw in and out to fix the problem, but no luck. it only seems to be at less than half throttle.
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Trailmaster XRX 150 TK Variator and 1500 Spring SYC Performance Ported & Polished & Shaved 2 Valve Head, A-10 Camshaft, R2C Filter, and Hammerhead Exhaust Hammerhead 250GTS White Torque and Clutch Springs, 18g Rollers, R2C Filter, Ported Polished and Shaved Head, Hammerhead Exhaust |
#2
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what does the plug look like? Black, brown or white?
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HH GTS 250 HH GT 150 Kandi Spyder 250 |
#3
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by half throttle, it should be running on the main jet. maybe try adjusting the needle lower to reduce the amount of fuel at that position. if the plug is showing rich, maybe too big of a main.
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#4
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You nearly never need to change a pilot jet from its stock value. Change it back and see how it runs.
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#5
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Sorry guys. This issue has been fixed and buggy sold since that time. Thanks for the input though.
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Trailmaster XRX 150 TK Variator and 1500 Spring SYC Performance Ported & Polished & Shaved 2 Valve Head, A-10 Camshaft, R2C Filter, and Hammerhead Exhaust Hammerhead 250GTS White Torque and Clutch Springs, 18g Rollers, R2C Filter, Ported Polished and Shaved Head, Hammerhead Exhaust |
#6
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Well ... what was it anyway? Always good to report in case someone else runs into the same issue.
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#7
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If I remember correctly it was the valve lashings and the old carb. Once I reinstalled the head I had a heck of a time adjusting the valves. Once the valve cover was tightened down the adjusters couldn't be moved. I had to loosen the valve cover and adjust the valves while it was running. I also replaced the carb and all issues went away and it ran like a wild banshee.
Hopefully I won't have any issues with this newly modded Hammerhead 250 GTS I just got from Tom today.
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Trailmaster XRX 150 TK Variator and 1500 Spring SYC Performance Ported & Polished & Shaved 2 Valve Head, A-10 Camshaft, R2C Filter, and Hammerhead Exhaust Hammerhead 250GTS White Torque and Clutch Springs, 18g Rollers, R2C Filter, Ported Polished and Shaved Head, Hammerhead Exhaust |
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