BuggyMasters.Com - An On Line Mini Buggy Forum and Go Kart Forum

Go Back   BuggyMasters.Com - An On Line Mini Buggy Forum and Go Kart Forum > Technical Discussions > 150cc GY6 and Under Engine Tech

150cc GY6 and Under Engine Tech GY6 and Smaller Technical Discussion Forum

 
 
Thread Tools
  #1  
Old 10-23-2014, 07:11 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Question VM 26 tuning

Yes, I'm full of issues today. So, I put in my new Mikuni VM26-606 and it fired right up with the choke off. Will die instantly if I put the choke on. Motor is a 4V 155cc GY6 I'm at sea level running 20 pilot, 175 main, 60 degrees F, 110 octane leaded race fuel... This is an indication of too big a pilot, correct? Couldn't mess with it too much due to electrical problem detailed in another post
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B

Last edited by wildbob; 10-23-2014 at 07:17 PM.
  #2  
Old 10-23-2014, 11:32 PM
xlint89's Avatar
xlint89 xlint89 is offline
Senior Member
 

Join Date: Dec 2011
Location: cleveland OH
Posts: 1,064
Default

Not sure why you're worried about the choke. If it starts up without it, why apply it?

How is acceleration? Would be my question.
__________________
My Yerban assault vehicle: 2.2mm stroker crank, 62mm Nikasil cyl, Taida large vavle head, American made valve springs, ported intake manifold, TM 28mm carb, stock CDI, Bando coil, TK exhaust, stock CVT except for the 14g sliders, 13/40 internal gears, 16T drive, 31T axle sprocket, 22" rear tires, and ONE BIG POTATO CANNON mounted on top..........
  #3  
Old 10-24-2014, 08:10 AM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

Yeah, just going by the tuning guide. Won't be able to test it until I solve my weird electrical problem.. Something shorting out when I crank the motor and melting the ground wire that goes from the harness to the CVT bolt..Like, full on smoke and stuff..not good..
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #4  
Old 10-24-2014, 06:40 PM
xlint89's Avatar
xlint89 xlint89 is offline
Senior Member
 

Join Date: Dec 2011
Location: cleveland OH
Posts: 1,064
Default

Check your negative battery cable, connector, and connection.

Sounds like alot of amps are trying to travel through your small gauge wire causing it to melt down.
__________________
My Yerban assault vehicle: 2.2mm stroker crank, 62mm Nikasil cyl, Taida large vavle head, American made valve springs, ported intake manifold, TM 28mm carb, stock CDI, Bando coil, TK exhaust, stock CVT except for the 14g sliders, 13/40 internal gears, 16T drive, 31T axle sprocket, 22" rear tires, and ONE BIG POTATO CANNON mounted on top..........
  #5  
Old 10-24-2014, 06:59 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

Hmm.. ok.. the cable was new (as the old one melted), but I'll clean all the connections.. I did a test crank when I got home and it fired right up without a issue.. I'll take a look at the connections..
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #6  
Old 10-25-2014, 07:25 AM
xlint89's Avatar
xlint89 xlint89 is offline
Senior Member
 

Join Date: Dec 2011
Location: cleveland OH
Posts: 1,064
Default

Silly question, but I have to ask....

Are the wires you're replacing the same gauge (size) or bigger than OEM?

I'm sure you already did, but also look for any chafed/pinched wires, or burn marks from an elec arc.

If it was water that seems to have started this issue, maybe disconnect all your elec connections, make sure it's dry and add some dielectric grease to them to keep water out.

By doing that, I'm hoping you will inspect all of your elec system and maybe find the source of your problem.
__________________
My Yerban assault vehicle: 2.2mm stroker crank, 62mm Nikasil cyl, Taida large vavle head, American made valve springs, ported intake manifold, TM 28mm carb, stock CDI, Bando coil, TK exhaust, stock CVT except for the 14g sliders, 13/40 internal gears, 16T drive, 31T axle sprocket, 22" rear tires, and ONE BIG POTATO CANNON mounted on top..........
  #7  
Old 10-25-2014, 12:31 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

You may be right.. Negative terminal was a bit loose. Tightened it up and seems to have corrected the problem..
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #8  
Old 10-25-2014, 03:32 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

Yup..I think you were right on.. Probably wasn't even the water the first time...
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #9  
Old 10-25-2014, 04:39 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

Just waiting on the correct throttle cable to arrive....
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #10  
Old 10-25-2014, 10:00 PM
351mustanger 351mustanger is offline
Contributor
 

Join Date: Jul 2013
Location: Cincinnati, Ohio
Posts: 160
Default

Quote:
Originally Posted by xlint89 View Post
Not sure why you're worried about the choke. If it starts up without it, why apply it?

How is acceleration? Would be my question.
If it starts cold without the choke, it is rich.

I don't know if you have found this yet.
http://www.mikunioz.com/vm_tuning_manual.htm

Last edited by 351mustanger; 10-25-2014 at 10:03 PM.
  #11  
Old 10-26-2014, 01:43 AM
xlint89's Avatar
xlint89 xlint89 is offline
Senior Member
 

Join Date: Dec 2011
Location: cleveland OH
Posts: 1,064
Default

Nice find 351.

You're prob right about the choke thing, but mine starts up without the choke (TM 28) and takes off great. So I don't mess with it
__________________
My Yerban assault vehicle: 2.2mm stroker crank, 62mm Nikasil cyl, Taida large vavle head, American made valve springs, ported intake manifold, TM 28mm carb, stock CDI, Bando coil, TK exhaust, stock CVT except for the 14g sliders, 13/40 internal gears, 16T drive, 31T axle sprocket, 22" rear tires, and ONE BIG POTATO CANNON mounted on top..........
  #12  
Old 10-26-2014, 10:19 AM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

So, the theory would be that my pilot jet is too big, correct? I'm still waiting for a throttle cable so I can't work on issues past idle.. Yes, I have the tuning guide, but thank you!!!
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #13  
Old 10-26-2014, 03:05 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

threw in a 17.5 pilot.. I'll try it out in a little while.. The Pats are on..
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #14  
Old 05-16-2015, 04:06 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

Hi Folks,
Back from some army stuff. still boggy with a 17.5 pilot. fires right up without the choke, no-go with choke on.
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #15  
Old 05-17-2015, 08:08 AM
jmansracerocket's Avatar
jmansracerocket jmansracerocket is offline
Senior Member
 

Join Date: Apr 2012
Location: ny, long island
Posts: 1,342
Default

Sounds like then it's to big of a pilot jet or maybe try turning the fuel mixture screw in ?
__________________
Hammer head Single seater know as herbie
under construction

Aluminum fuel tank, aluminum wheels, custom fuel/cargo rack, entire rewire, trail tech vapor, ported big valve head, a12camshaft, 12 gram sliders, straight intake, kirkey wide seat, front end extension. 4 point harness, welded cage. Hammerhead exhaust.



Blade Single Seater Restore
welded cage, engine build, new wiring harness/electric box, spun aluminum fuel tank.
  #16  
Old 05-18-2015, 11:56 AM
tkeagle tkeagle is offline
Heavy Contributor
 

Join Date: Mar 2015
Location: Central Kansas
Posts: 556
Default

I have the same carb. On yd gy6. 155cc. 1500 feet roughly. Only half to use the choke when air temp. Gets in 50's or below. Even then only need to choke it once on full choke. Will die shortly. Then take choke off and fires up. If try to choke after its running. Will die. I haven't changed the jets. Using stock ones it came with. That being said I believe at lower throttle I think I'm slightly rich. But mid, and WOT. spark plug check looks good. It does bog slightly on take off. I've read that down jetting would be best for current setup. (Even with A12 cam..high flow intake and exhaust. Which I have.) The stock jets are good once you get into the 175 Bb. Kits. But I don't have 4V. So not sure how that applies in your case. But sounds like your setup with that carb. Reacts much like mine does. Plan on getting a 175 bb kit. Its not running so rich that I think its a big issue. Since do want to up grade. But if I wasn't going to upgrade, I'd go ahead and down.
  #17  
Old 05-30-2015, 06:28 PM
hhgtsplatinum's Avatar
hhgtsplatinum hhgtsplatinum is offline
Lite Contributor
 

Join Date: Jan 2015
Location: georgia
Posts: 98
Default

hey guys I am currently changing my carb also, I have a hammerhead and I am going from a cvk 24 to a oko flat slide 26mm. I am just wondering as my carb came with two extra sets of jets and pilots yet still none of them (the two extra sets and the ones installed) have any numbers on them. on my 24mm I had to go up on the pilot from a 35 to a 38 and up on the jet from a 111 stock to a 130... do you guys have any tips on carb adjusting?
__________________
Hammerhead GTS150 Platinum
PnP Head, A12 Cam, Uni Filter with aluminum intake tube, Custom Straight through Exhaust, hp coil and ngk plug, 11G sliders, 2000 Contra Spring, 1000 Clutch Springs, ITP tires, winch. 130 main Jet, 38 pilot
  #18  
Old 05-31-2015, 09:49 AM
SYCARMS's Avatar
SYCARMS SYCARMS is offline
Supporting Vendor
 

Join Date: Sep 2009
Location: Senatobia, Mississippi
Posts: 3,375
Default

You need a base line to tune from. Being that you have un numbered jets you don't have a baseline. The slide carbs tune differently than a CV carb in that not only will you be changing out the jets but also needle, needle seat and in some instances the barrel slide. When a slide carb is used on say a Honda dirt bike the factory will tune that carb for the bike. Unlike a cv carb If you have the same size carb on say a Honda and KTM bike of same cc engine they could be tuned totally different since a slide carb is more of a custom tuned carb as compared to a cv carb which is universal. Not only do the jets need to be numbered also does the barrel slide, needle, and needle seat. If not you will be shooting in the dark. Also a flat slide is more difficult to tune than a round slide. I would return that carb to get one that is numbered properly. Or you can spend the extra money for a Mikuni VM26 series 606. I would also pick up a book which instructs how to tune. They require more to tune but when tuned properly, performance is unmatched as compared to a cv carb. Also a flat slide is more temperamental to elevation, temperature and humidity as compared to a round slide.
  #19  
Old 05-31-2015, 06:14 PM
hhgtsplatinum's Avatar
hhgtsplatinum hhgtsplatinum is offline
Lite Contributor
 

Join Date: Jan 2015
Location: georgia
Posts: 98
Default

O ok thanks, man sounds like a alot of work but i want to learn how to tune carbs and all, i want to learn these bad boys inside and out, thanks! I think i'll order me some jets so i ca have a good starting point
__________________
Hammerhead GTS150 Platinum
PnP Head, A12 Cam, Uni Filter with aluminum intake tube, Custom Straight through Exhaust, hp coil and ngk plug, 11G sliders, 2000 Contra Spring, 1000 Clutch Springs, ITP tires, winch. 130 main Jet, 38 pilot
  #20  
Old 07-13-2015, 07:38 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

Just to cap this thread off, I'd mis-measured the float level on the new carb. It was off right out of the box. Got it back in spec and it seems to run pretty good. I've just ripped up and down the street a few times, but I should be able to do a real plug check this weekend and get it dialed in. Currently #15 Pilot, #145 main, clip one down on the needle, sea level, running 110 leaded fuel.. CHECK YER FLOATS!!! I ended up making my own harness to correct my electrical woes.
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B

Last edited by wildbob; 07-13-2015 at 08:54 PM.
  #21  
Old 07-14-2015, 09:23 AM
liduno liduno is offline
Heavy Contributor
 

Join Date: Aug 2014
Posts: 702
Default

Unless you have a high compression motor, the 110 is probably hurting performance. The higher the octane the slower the burn.
  #22  
Old 07-14-2015, 09:28 AM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

Good to know. I get it for free and it's pre-stabilized though..
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #23  
Old 07-14-2015, 10:28 AM
liduno liduno is offline
Heavy Contributor
 

Join Date: Aug 2014
Posts: 702
Default

Quote:
Originally Posted by wildbob View Post
Good to know. I get it for free and it's pre-stabilized though..
Free is good..lol
  #24  
Old 07-14-2015, 10:55 AM
SYCARMS's Avatar
SYCARMS SYCARMS is offline
Supporting Vendor
 

Join Date: Sep 2009
Location: Senatobia, Mississippi
Posts: 3,375
Default

If you mixed equal parts of the 110 with some non ethanol 87 you would have a manageable 98.5 octane. Also keep in mind that if using avgas it is blended to burn at high altitude(less O2) so at sea-level(more O2) it will run lean.
  #25  
Old 07-14-2015, 12:03 PM
liduno liduno is offline
Heavy Contributor
 

Join Date: Aug 2014
Posts: 702
Default

Quote:
Originally Posted by SYCARMS View Post
If you mixed equal parts of the 110 with some non ethanol 87 you would have a manageable 98.5 octane. Also keep in mind that if using avgas it is blended to burn at high altitude(less O2) so at sea-level(more O2) it will run lean.
I have heard stories of guys blowing up their motors using aviation fuel. I wonder if jetting would fix that problem?
  #26  
Old 07-14-2015, 12:08 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

I'm using sunoco standard race fuel, maybe a bit of a blend would work nice. Just don't blend my scotch!!
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #27  
Old 07-14-2015, 01:50 PM
SYCARMS's Avatar
SYCARMS SYCARMS is offline
Supporting Vendor
 

Join Date: Sep 2009
Location: Senatobia, Mississippi
Posts: 3,375
Default

Wish I had access to free Sunoco 110 octane fuel. Last time I come back from Chicago my Son noticed when we stopped to fuel that they had Sunoco 110 @$7.90 / gallon. I had a 5 gal can in the truck and purchased another at the WalMart next door and got 10 gallons. Down here all I have access to is either VP or Renegade for $15 plus at the speed shops.
  #28  
Old 07-14-2015, 03:30 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

Yeah, it's not a bottomless supply and they sell it at the pump 20 minutes away from where I live..
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #29  
Old 07-24-2015, 02:53 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

Didn't get too much testing done last weekend. Throttle kept sticking open like the slide spring was binding or something, and couldn't get it to idle below 900rpm. I had my buddy steer it while I towed it back to the campsite with my truck, rolled it on the trailer and decided to spend the rest of my weekend over-indulging in adult beverages.. I'll take it all apart and maybe get some testing done this weekend..
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #30  
Old 07-25-2015, 12:37 PM
SYCARMS's Avatar
SYCARMS SYCARMS is offline
Supporting Vendor
 

Join Date: Sep 2009
Location: Senatobia, Mississippi
Posts: 3,375
Default

Wise to have a backup plan. Buggy breaks ! Out come the adult beverages.
  #31  
Old 07-25-2015, 02:14 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

Yeah, I'd left it in gear so when I started it to test, off it went at full throttle, me diving in getting dragged like a cowboy with his hands caught in the reigns.. I think with all the taking the carbs on and off I might have stripped one of the clamps on the connector to the intake and I'm getting some air leak.. surges up and down and won't idle below about 800rpm..
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #32  
Old 07-25-2015, 02:34 PM
jmansracerocket's Avatar
jmansracerocket jmansracerocket is offline
Senior Member
 

Join Date: Apr 2012
Location: ny, long island
Posts: 1,342
Default

Quote:
Originally Posted by wildbob View Post
Yeah, I'd left it in gear so when I started it to test, off it went at full throttle, me diving in getting dragged like a cowboy with his hands caught in the reigns.. I think with all the taking the carbs on and off I might have stripped one of the clamps on the connector to the intake and I'm getting some air leak.. surges up and down and won't idle below about 800rpm..
hahahah I can laugh at this because this had happened to me a year or 2 ago started the yerf when not sitting in it and it took off on me and it just dragged me with it so now I don't start unless im in it.
__________________
Hammer head Single seater know as herbie
under construction

Aluminum fuel tank, aluminum wheels, custom fuel/cargo rack, entire rewire, trail tech vapor, ported big valve head, a12camshaft, 12 gram sliders, straight intake, kirkey wide seat, front end extension. 4 point harness, welded cage. Hammerhead exhaust.



Blade Single Seater Restore
welded cage, engine build, new wiring harness/electric box, spun aluminum fuel tank.
  #33  
Old 07-25-2015, 06:10 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

I'm a dummy. I've had so much trouble getting this carb to work, I'd stopped looking at other parts on the throttle system. The adjuster near the gas pedal was all out of whack. Getting there. idle-25% throttle awesome, bogs and sputters mid throttle, runs like a champ 60%-WOT.
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #34  
Old 07-26-2015, 12:10 AM
x-bird's Avatar
x-bird x-bird is offline
Power User
 

Join Date: Oct 2011
Location: Penciltucky
Posts: 2,518
Default

if everything in the carb is clean, try dropping the needle all the way in the hole and tune with the fuel screw. If you cant get rid of the mid range bog, then maybe go down one size on the main jet and bring the needle up to the middle notch .
  #35  
Old 07-26-2015, 08:26 AM
SYCARMS's Avatar
SYCARMS SYCARMS is offline
Supporting Vendor
 

Join Date: Sep 2009
Location: Senatobia, Mississippi
Posts: 3,375
Default

You need to do a full throttle run, 900-1200ft. with throttle wide open. At end of run with throttle still to the floor cut the ignition. When engine stops close throttle, pull over, pull plug and read. Doing it this way tells you if main jet is too rich, lean or just right and takes the pilot jet out of the picture. Once you have the main jet just right then you can work on the pilot jet. When I done mine I had the clip on needle half way. Getting the main jet correct first makes tuning much easier and assures you the engine will not lean out at full throttle.
  #36  
Old 07-26-2015, 01:48 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

Yep, now that I have it running well enough (and safely enough) I can do a plug test. probably next weekend for that however. I got a bag of new plugs for testing and some good ones for when it's dialed in.
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #37  
Old 07-26-2015, 04:25 PM
SYCARMS's Avatar
SYCARMS SYCARMS is offline
Supporting Vendor
 

Join Date: Sep 2009
Location: Senatobia, Mississippi
Posts: 3,375
Default

You don't want a new plug. Use an old plug it will show color better.
  #38  
Old 07-27-2015, 07:56 AM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

Oh, cool. For some reason I thought you needed new plugs. good to know.
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #39  
Old 07-31-2015, 04:28 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

Ha, looks like I did strip the clamps on the intake. Went to do some tuning today and my airfilter/intake stack kept coming off the carb. Tough to get it tuned with no air filter on.. Now to find where it fell off..

EDIT: $4.21 for four new No.24 clamps at NAPA..back to the dirt in a bit.
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #40  
Old 08-01-2015, 02:01 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

As it REALLY turns out, my new rear shocks were too soft and bottoming out causing the cargo rack to smack my stack and filter off the carb. Wrenched down the preload on the shocks as my as I could in the woods, and got some good runs in. After getting the floats right, I had to jet way up. currently #20 pilot and #180 main. Needle clip in the middle. Runs Awesome idle to 35%, Stumble/crackle/bog 35%-45%, and runs like a monster there to 100%. I just need to get that one pre-mid throttle area smoothed out, and I'll be good to go.
Attached Images
File Type: jpg plug.jpg (85.1 KB, 5 views)
File Type: jpg plug2.jpg (87.8 KB, 4 views)
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B

Last edited by wildbob; 08-01-2015 at 02:04 PM.
  #41  
Old 08-02-2015, 09:06 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

and as it turns out my needle is bent. That's why my carb was sticking open. The needle wouldn't go back into it's seat.. Holy crap.
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
  #42  
Old 09-03-2015, 03:28 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

Buggy is running pretty good. I seem to have lost some top end, so I might bump up the main..
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
 


Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off

Forum Jump


All times are GMT -5. The time now is 08:35 PM.


Powered by vBulletin® Version 3.8.3
Copyright ©2000 - 2024, Jelsoft Enterprises Ltd.