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Electrical Tech General Tech for Electrical issues not related to specific engines (Lights etc)

 
 
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  #1  
Old 10-23-2014, 07:01 PM
wildbob wildbob is offline
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Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Unhappy weird electrical problem

So three weeks or so ago I was blasting around in the rain, big puddles etc.. buggy was soaked but running fine.. Went back to the campsite for a while and an hour or so later got back on it to got for a spin.. Went to crank the motor and it barely would turn over, like the battery was almost dead.. My buddy saw smoke coming out of my electrical box.. after I got it home I opened up the box and found the ground wire from the harness (that attaches to one of the CVT cover bolts) was melted.. So, i bought a new stator (green wire from that looked a bit melted too), and a new harness. Got my new VM26 carb on today and it started right up. Shut it off to fool with the jetting, and when I cranked it up again, motor barely would crank and ground wire heated up and started smoking again.. Wires only heat up when I crank the starter, not while it's running.. Any ideas?
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2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B

Last edited by wildbob; 10-23-2014 at 08:50 PM.
  #2  
Old 10-25-2014, 04:36 PM
wildbob wildbob is offline
Heavy Contributor
 

Join Date: Aug 2013
Location: Newburyport, MA
Posts: 571
Default

Xlint89 hit it on the head I think.. Negative terminal connection to battery was loose, sending mondo amps down the ground wire..
__________________
2013 Trailmaster XRX 150 Type 86 stroker
Taida 4V head with 23/22mm valves, forged 4V piston,Taida 62mm jug,forged Taida 8200 KDU stroker crank, Koso high-flow oil pump, Taida case half w/ oil cooler ports, Setrab oil cooler,TrailTec Vapor, Mikuni VM26-606, aluminum 30mm intake, Uni filter, aluminum stack, Hammerhead racing exhaust, MotoRio adjustable CDI/HO Coil, Iridium plug, Full Dr Pulley CVT kit w/ 16g sliders, JD's Mikuni slide kit

2014 Kandi 90B
 


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